FTC 7314 Engineering Notebook 2016-02-06

From DEW Robotics
Revision as of 20:54, 6 February 2016 by Aberge00 (talk | contribs) (Mechanical)

Jump to: navigation, search

Competition Season Meeting

Meeting Date Meeting Time Location Attendees
TCHS Brandywine

CAD & Design

Mechanical

-Fixing Debris Loss On Mountain

-Myles thought of ideas for keeping debris from flying out the mountain, he then tested them on the robot.

-Fixing the Tread Bearing

-Bennett helped Matt push out a tread bearing that had sunk in too far into the arm frame.

-Re-soldering the Beacon Battery Holster

-Snarr prepared his work space for re-soldering a loose wire that connects to the beacon battery holster. He soldered the wire back to the holster and the beacon worked afterwards.

-

Programming

Field Elements



Recorded by: Date: Journal Editor: Date: