FTC 7314 Engineering Notebook 2016-02-06
From DEW Robotics
Revision as of 21:02, 6 February 2016 by Aberge00
Competition Season Meeting
|Meeting Date||Meeting Time||Location||Attendees|
CAD & Design
-Fixing Debris Loss On Mountain
- -Myles thought of ideas for keeping debris from flying out the mountain, he then tested them on the robot.
-Fixing the Tread Bearing
- -Bennett helped Matt push out a tread bearing that had sunk in too far into the arm frame.
- -Matt help trouble shoot to see what was causing the problem of keeping the robots arm from properly raising and lowering. Matt also fixed the arm and removed the thing that was keeping the arm from raising and lowering
-Re-soldering the Beacon Battery Holster
- -Snarr prepared his work space for re-soldering a loose wire that connects to the beacon battery holster. He soldered the wire back to the holster and the beacon worked afterwards.
|Recorded by:||Date:||Journal Editor:||Date:|