Difference between revisions of "Stronghold Meeting -15-Feb-2016"
From DEW Robotics
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==Programming== | ==Programming== | ||
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+ | -We finally got our practice robot up and running! | ||
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+ | :- We assigned IDs to each CAN talon, and updated the code to match. | ||
+ | |||
+ | :- We also added a thread for the portcullis lift, and linked the pneumatic to the left bumper. | ||
==Strategy== | ==Strategy== |
Latest revision as of 19:28, 16 February 2016
Contents
Competition Season Meeting
Meeting Date | Meeting Time | Location | Attendees |
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TCHS Brandywine |
CAD & Design
Today we discovered the real reason we CAD everything before it is built... That's right. We messed up. The motor powering our intake system is misplaced, and prohibits the mechanism from actually running. Now we are trying to fix our mistakes. GrabCAD is giving us some issues, and we've lost the changes that we made for a possible solution.
Mechanical
Programming
-We finally got our practice robot up and running!
- - We assigned IDs to each CAN talon, and updated the code to match.
- - We also added a thread for the portcullis lift, and linked the pneumatic to the left bumper.
Strategy
Field Elements
Other
Recorded by: | Date: | Journal Editor: | Date: |
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